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authorIgor Grinberg <grinberg@compulab.co.il>2011-05-09 14:41:46 +0300
committerGreg Kroah-Hartman <gregkh@suse.de>2011-08-08 10:23:10 -0700
commit122c9c81347704a14db5a7d87b14165cdd7d496e (patch)
tree9d7bf320fe01cc39d3d10efcc167481aaadd0c1e /arch
parentb43906bf751f5d8f26425a809806bbc1b6a33422 (diff)
ARM: pxa/cm-x300: fix V3020 RTC functionality
commit 6c7b3ea52e345ab614edb91d3f0e9f3bb3713871 upstream. While in sleep mode the CS# and other V3020 RTC GPIOs must be driven high, otherwise V3020 RTC fails to keep the right time in sleep mode. Signed-off-by: Igor Grinberg <grinberg@compulab.co.il> Signed-off-by: Eric Miao <eric.y.miao@gmail.com> Signed-off-by: Greg Kroah-Hartman <gregkh@suse.de>
Diffstat (limited to 'arch')
-rw-r--r--arch/arm/mach-pxa/cm-x300.c8
1 files changed, 4 insertions, 4 deletions
diff --git a/arch/arm/mach-pxa/cm-x300.c b/arch/arm/mach-pxa/cm-x300.c
index 102916f1e46..b6bfe7e2695 100644
--- a/arch/arm/mach-pxa/cm-x300.c
+++ b/arch/arm/mach-pxa/cm-x300.c
@@ -143,10 +143,10 @@ static mfp_cfg_t cm_x300_mfp_cfg[] __initdata = {
GPIO99_GPIO, /* Ethernet IRQ */
/* RTC GPIOs */
- GPIO95_GPIO, /* RTC CS */
- GPIO96_GPIO, /* RTC WR */
- GPIO97_GPIO, /* RTC RD */
- GPIO98_GPIO, /* RTC IO */
+ GPIO95_GPIO | MFP_LPM_DRIVE_HIGH, /* RTC CS */
+ GPIO96_GPIO | MFP_LPM_DRIVE_HIGH, /* RTC WR */
+ GPIO97_GPIO | MFP_LPM_DRIVE_HIGH, /* RTC RD */
+ GPIO98_GPIO, /* RTC IO */
/* Standard I2C */
GPIO21_I2C_SCL,